I installed it two years ago and it ripped right from the beginning - 15lbs - 124 mph (more than gearing was suppose to allow) on GPS and I put 1000 + miles on it until one day when I was out of race fuel/93 mix and stupidly I ran it too hard.
Rebuilt with low compression pistons.
Put it back together with all settings the same. 500 jet in the Pitot tube. Stock jetting in the carbs and a Hallman Boost controller that has 14 full turns and I have it turned in 8 turns. Rebuilt it at the end of that season and rode it 1 time and it wasn't right but put it away for the summer to work on it later.
I got into ice oval racing the next year and it sat all year and never ran it. This year I just got it out to run for a few days in Michigan. I pulled the carbs, removed all the jets, cleaned them throroughly with mini pipe cleaning tools, flushed the tank of old gas and put in a 1/2 mix of 93 non-ox and 110.
It still did the same thing as after I rebuilt it - If I put the throttle to the bar, she falls on her face and spits and pops real bad. I tried a leaner pitot to 740 and it barely helped. If I run 1/2 to 2/3 throttle it picks up fine and builds boost to a point - I can get 8 lbs on the guage (with my controller turned all the way out - if I turn it in, everything gets worse) but it feels like it is running on maybe 4 lbs. IF I go past that 2/3 rds, it spits and pops. Almost like it will build boost so far and then just give up.
I found one of the little o-rings in the top of a carb missing, replaced it, didn't help. I have the billet tee's, checked the connections and bender box for cracks, can't seem to find anything. Haven't pressure tested yet.
I was told I need to go leaner with low comp pistons but would it really make it act that bad?
My suspicion is a leak somewhere but I am curious as to what the experts think. Should I try lower mains first?
Thanks in advance for the help, I have read a lot of threads and haven't seen anything quite the same.
Forgot to say - it is an 05 RX1, does have a BOV located shortly after the Pitot towards the intercooler.
Rebuilt with low compression pistons.
Put it back together with all settings the same. 500 jet in the Pitot tube. Stock jetting in the carbs and a Hallman Boost controller that has 14 full turns and I have it turned in 8 turns. Rebuilt it at the end of that season and rode it 1 time and it wasn't right but put it away for the summer to work on it later.
I got into ice oval racing the next year and it sat all year and never ran it. This year I just got it out to run for a few days in Michigan. I pulled the carbs, removed all the jets, cleaned them throroughly with mini pipe cleaning tools, flushed the tank of old gas and put in a 1/2 mix of 93 non-ox and 110.
It still did the same thing as after I rebuilt it - If I put the throttle to the bar, she falls on her face and spits and pops real bad. I tried a leaner pitot to 740 and it barely helped. If I run 1/2 to 2/3 throttle it picks up fine and builds boost to a point - I can get 8 lbs on the guage (with my controller turned all the way out - if I turn it in, everything gets worse) but it feels like it is running on maybe 4 lbs. IF I go past that 2/3 rds, it spits and pops. Almost like it will build boost so far and then just give up.
I found one of the little o-rings in the top of a carb missing, replaced it, didn't help. I have the billet tee's, checked the connections and bender box for cracks, can't seem to find anything. Haven't pressure tested yet.
I was told I need to go leaner with low comp pistons but would it really make it act that bad?
My suspicion is a leak somewhere but I am curious as to what the experts think. Should I try lower mains first?
Thanks in advance for the help, I have read a lot of threads and haven't seen anything quite the same.
Forgot to say - it is an 05 RX1, does have a BOV located shortly after the Pitot towards the intercooler.